Download DN256 - 1.4MHz Switching Regulator Draws Only 10µA Supply Current

Survey
yes no Was this document useful for you?
   Thank you for your participation!

* Your assessment is very important for improving the workof artificial intelligence, which forms the content of this project

Document related concepts

Electrical substation wikipedia , lookup

Electrification wikipedia , lookup

History of electric power transmission wikipedia , lookup

Heterodyne wikipedia , lookup

Multidimensional empirical mode decomposition wikipedia , lookup

Power inverter wikipedia , lookup

Induction motor wikipedia , lookup

Mercury-arc valve wikipedia , lookup

Three-phase electric power wikipedia , lookup

Islanding wikipedia , lookup

Rectifier wikipedia , lookup

Voltage regulator wikipedia , lookup

Resistive opto-isolator wikipedia , lookup

Power electronics wikipedia , lookup

TRIAC wikipedia , lookup

Alternating current wikipedia , lookup

Current source wikipedia , lookup

Two-port network wikipedia , lookup

Variable-frequency drive wikipedia , lookup

Pulse-width modulation wikipedia , lookup

Current mirror wikipedia , lookup

Switched-mode power supply wikipedia , lookup

Opto-isolator wikipedia , lookup

Buck converter wikipedia , lookup

Transcript
advertisement
1.4MHz Switching Regulator Draws Only 10µA Supply Current
Design Note 256
Jaime Tseng
Introduction
High switching frequency and low quiescent current are
no longer conflicting requirements in the design of battery-powered products. Linear Technology’s LTC®3404 is
the industry’s first step-down switching regulator that
operates at 1.4MHz while drawing only 10µA of supply
current (using Burst ModeTM operation) at no load. This
impressive feat allows for better than 90% efficiency over
three decades of output load current while allowing the
use of tiny external components. With the on-chip main
and synchronous switches, minimal external components are necessary to make a complete, high efficiency
(up to 95%) step-down regulator. Tiny external components and the LTC3404’s MSOP package provide a minimum-area solution to meet the limited space requirements
of today’s portable applications.
driving SYNC/MODE pin HIGH with a logic-level signal or
by tying it to VIN. For lower noise, pulse skipping mode can
be selected by driving the SYNC/MODE pin LOW with a
logic-level signal or by tying it to ground. In this case,
constant-frequency operation is maintained at lower load
currents together with minimum output ripple. If the load
current is low enough, cycle skipping will eventually occur
to maintain regulation. In this mode, the efficiency will be
lower at very light loads, but becomes comparable to
Burst Mode operation when the output load exceeds
50mA. For switching-frequency-sensitive applications,
the LTC3404 can be externally synchronized to frequencies from 1MHz to 1.7MHz by applying an external clock
signal to the SYNC/MODE pin. During synchronization,
Burst Mode operation is inhibited and pulse skipping
mode is selected.
LTC3404 Features
The LTC3404 incorporates a constant-frequency, current
mode architecture that provides low noise and fast transient response. Its input voltage supply range of 2.65V to
6V and 100% duty cycle capability for low dropout make
the LTC3404 ideal for moderate current (up to 600mA)
battery-powered applications.
3.1V/600mA Step-Down Regulator
Figure 1 shows a typical application suitable for a single
Li-Ion cell or 3- to 4-cell NiCd or NiMH battery input. Note
the small component values used in this application,
made possible by the high switching frequency of the
LTC3404. Also, because of the part’s internal synchronous switch, the Schottky diode normally seen on the SW
pin is absent from Figure 1. This regulator occupies only
0.47" x 0.31" (0.146in2) of board area.
For maximum efficiency over the widest range of output
load current, Burst Mode operation can be selected by
LTC3404
1
2
3
4
RUN
ITH
PLL LPF
SYNC/MODE
VFB
VIN
GND
SW
8
10µF†
CER
100
7
VIN = 3.6V
95
6
5 4.7µH*
VOUT††
3.1V
22µF**
CER
887k
DN261 F01
309k
, LTC and LT are registered trademarks of Linear Technology Corporation.
Burst Mode is a trademark of Linear Technology Corporation.
EFFICIENCY (%)
47pF
VIN
2.65V
TO 6V
90
VIN = 4.2V
85
VIN = 6V
80
22pF
75
VOUT = 3.1V
(847) 649-3430
*TOKO A914BYW-4R7M
(770) 436-1300
**MURATA GRM42-6X5R226K6.3
†MURATA GRM42-6X5R106K6.3
††V
OUT CONNECTED TO VIN FOR 2.65V < VIN < 3.1V
Figure 1. 3.1V/600mA Step-Down Regulator
05/01/256
70
0.1
1.0
10
LOAD (mA)
100
1000
DN261 F02
Figure 2. Efficiency vs Load Current for Figure 1’s Circuit
(Burst Mode Operation Enabled)
www.BDTIC.com/Linear
Figure 2 shows the efficiency for three different input
voltages. The efficiency for a 3.6V input exceeds 90% over
three decades of output current. The efficiency remains
high down to loads as small as 100µA due to the LTC3404’s
ultralow quiescent current. Even though the quiescent
current is very low, the transient performance is not compromised. Innovative new circuitry ensures that the error
amplifier, while operating on less than 10µA at no load,
can quickly respond to load changes. The oscilloscope
photo in Figure 3 shows the part’s outstanding transient
performance when subjected to a 600mA load step. Note
how the inductor current ripple is reduced as the load step
forces continuous switching operation from Burst Mode
operation. At maximum output load, the inductor current
ripple is at its lowest due to the increased duty cycle caused
by the IR drop of the main switch.
In this mode the efficiency is lower at light loads, as
shown in Figure 5. However, the efficiency becomes
comparable to that of Burst Mode operation when the
output load exceeds 50mA.
The LTC3404 uses an internal phase-locked loop circuit to
synchronize to an external signal. A voltage-controlled
oscillator and a phase detector comprise the phaselocked loop. Filter components CLP and RLP smooth out
the current pulses from the phase detector to provide a
stable input to the voltage controlled oscillator. These
components determine how fast the loop acquires lock.
With the components shown in Figure 4, the loop acquires
lock in about 100µs. When not synchronized to an external clock, the internal connection to the VCO is disconnected to prevent noise from altering the internal oscillator
frequency. The oscilloscope photo in Figure 6 shows the
transient performance with a 600mA load step.
100
VOUT
100mV/DIV
AC COUPLED
90
VIN = 3.6V
80
VIN = 4.2V
VO = 3.1V
LOAD STEP = 50mA TO 600mA
EFFICIENCY (%)
70
INDUCTOR
CURRENT
500mA/DIV
VIN
IN = 6V
VIN = 4.2V
60
50
40
30
20
100µs/DIV
VOUT = 3.1V
1.2MHz EXTERNALLY
SYNCHRONIZED
10
Figure 3. Load Step Response for Figure 1’s Circuit
0
0.1
Externally Synchronized 3.1V/600mA
Step-Down Regulator
Figure 4 shows an application for low switching-frequency noise. The LTC3404 is synchronized to an external clock signal whereby Burst Mode operation is disabled
automatically. This provides constant-frequency operation at lower load currents, reducing the ripple voltage.
LTC3404
1
2
47pF
3
4
PLL LPF
RUN
ITH
SYNC/MODE
VFB
VIN
GND
SW
8
7
6
5
100
1000
DN261 F05
Figure 5. Efficiency vs Load Current for Figure 4’s Circuit
(Burst Mode Operation Disabled)
VOUT
100mV/DIV
AC COUPLED
INDUCTOR
CURRENT
500mA/DIV
VIN = 4.2V
VO = 3.1V
LOAD STEP = 50mA TO 600mA
EXT CLOCK
1.2MHz
4.7µH*
COUT*
22µF
CER
VOUT*
3.1V
VIN
2.65V TO 6V
CIN*
10µF
CER
DN261 F04
22pF
10
LOAD (mA)
CLP
R
0.01µF LP
100k
887k
309k
1.0
*SEE FIGURE 1
Figure 4. Externally Synchronized 3.1V/600mA
Step-Down Regulator
Data Sheet Download
http://www.linear-tech.com/go/dnLTC3404
Linear Technology Corporation
100µs/DIV
Figure 6. Load Step Response for Figure 6’s Circuit
Conclusion
The LTC3404 demonstrates that high switching frequency
and low quiescent current can coexist, and thereby opens
up a world of new possibilities in the design of batterypowered products.␣
For literature on our Switching Regulators,
call 1-800-4-LINEAR. For applications help,
call (408) 432-1900, Ext. 2377
dn261f LT/TP 0501 375K • PRINTED IN THE USA
1630 McCarthy Blvd., Milpitas, CA 95035-7417
www.BDTIC.com/Linear
(408)432-1900 ● FAX: (408) 434-0507 ● www.linear-tech.com
 LINEAR TECHNOLOGY CORPORATION 2001