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Download DN256 - 1.4MHz Switching Regulator Draws Only 10µA Supply Current
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advertisement 1.4MHz Switching Regulator Draws Only 10µA Supply Current Design Note 256 Jaime Tseng Introduction High switching frequency and low quiescent current are no longer conflicting requirements in the design of battery-powered products. Linear Technology’s LTC®3404 is the industry’s first step-down switching regulator that operates at 1.4MHz while drawing only 10µA of supply current (using Burst ModeTM operation) at no load. This impressive feat allows for better than 90% efficiency over three decades of output load current while allowing the use of tiny external components. With the on-chip main and synchronous switches, minimal external components are necessary to make a complete, high efficiency (up to 95%) step-down regulator. Tiny external components and the LTC3404’s MSOP package provide a minimum-area solution to meet the limited space requirements of today’s portable applications. driving SYNC/MODE pin HIGH with a logic-level signal or by tying it to VIN. For lower noise, pulse skipping mode can be selected by driving the SYNC/MODE pin LOW with a logic-level signal or by tying it to ground. In this case, constant-frequency operation is maintained at lower load currents together with minimum output ripple. If the load current is low enough, cycle skipping will eventually occur to maintain regulation. In this mode, the efficiency will be lower at very light loads, but becomes comparable to Burst Mode operation when the output load exceeds 50mA. For switching-frequency-sensitive applications, the LTC3404 can be externally synchronized to frequencies from 1MHz to 1.7MHz by applying an external clock signal to the SYNC/MODE pin. During synchronization, Burst Mode operation is inhibited and pulse skipping mode is selected. LTC3404 Features The LTC3404 incorporates a constant-frequency, current mode architecture that provides low noise and fast transient response. Its input voltage supply range of 2.65V to 6V and 100% duty cycle capability for low dropout make the LTC3404 ideal for moderate current (up to 600mA) battery-powered applications. 3.1V/600mA Step-Down Regulator Figure 1 shows a typical application suitable for a single Li-Ion cell or 3- to 4-cell NiCd or NiMH battery input. Note the small component values used in this application, made possible by the high switching frequency of the LTC3404. Also, because of the part’s internal synchronous switch, the Schottky diode normally seen on the SW pin is absent from Figure 1. This regulator occupies only 0.47" x 0.31" (0.146in2) of board area. For maximum efficiency over the widest range of output load current, Burst Mode operation can be selected by LTC3404 1 2 3 4 RUN ITH PLL LPF SYNC/MODE VFB VIN GND SW 8 10µF† CER 100 7 VIN = 3.6V 95 6 5 4.7µH* VOUT†† 3.1V 22µF** CER 887k DN261 F01 309k , LTC and LT are registered trademarks of Linear Technology Corporation. Burst Mode is a trademark of Linear Technology Corporation. EFFICIENCY (%) 47pF VIN 2.65V TO 6V 90 VIN = 4.2V 85 VIN = 6V 80 22pF 75 VOUT = 3.1V (847) 649-3430 *TOKO A914BYW-4R7M (770) 436-1300 **MURATA GRM42-6X5R226K6.3 †MURATA GRM42-6X5R106K6.3 ††V OUT CONNECTED TO VIN FOR 2.65V < VIN < 3.1V Figure 1. 3.1V/600mA Step-Down Regulator 05/01/256 70 0.1 1.0 10 LOAD (mA) 100 1000 DN261 F02 Figure 2. Efficiency vs Load Current for Figure 1’s Circuit (Burst Mode Operation Enabled) www.BDTIC.com/Linear Figure 2 shows the efficiency for three different input voltages. The efficiency for a 3.6V input exceeds 90% over three decades of output current. The efficiency remains high down to loads as small as 100µA due to the LTC3404’s ultralow quiescent current. Even though the quiescent current is very low, the transient performance is not compromised. Innovative new circuitry ensures that the error amplifier, while operating on less than 10µA at no load, can quickly respond to load changes. The oscilloscope photo in Figure 3 shows the part’s outstanding transient performance when subjected to a 600mA load step. Note how the inductor current ripple is reduced as the load step forces continuous switching operation from Burst Mode operation. At maximum output load, the inductor current ripple is at its lowest due to the increased duty cycle caused by the IR drop of the main switch. In this mode the efficiency is lower at light loads, as shown in Figure 5. However, the efficiency becomes comparable to that of Burst Mode operation when the output load exceeds 50mA. The LTC3404 uses an internal phase-locked loop circuit to synchronize to an external signal. A voltage-controlled oscillator and a phase detector comprise the phaselocked loop. Filter components CLP and RLP smooth out the current pulses from the phase detector to provide a stable input to the voltage controlled oscillator. These components determine how fast the loop acquires lock. With the components shown in Figure 4, the loop acquires lock in about 100µs. When not synchronized to an external clock, the internal connection to the VCO is disconnected to prevent noise from altering the internal oscillator frequency. The oscilloscope photo in Figure 6 shows the transient performance with a 600mA load step. 100 VOUT 100mV/DIV AC COUPLED 90 VIN = 3.6V 80 VIN = 4.2V VO = 3.1V LOAD STEP = 50mA TO 600mA EFFICIENCY (%) 70 INDUCTOR CURRENT 500mA/DIV VIN IN = 6V VIN = 4.2V 60 50 40 30 20 100µs/DIV VOUT = 3.1V 1.2MHz EXTERNALLY SYNCHRONIZED 10 Figure 3. Load Step Response for Figure 1’s Circuit 0 0.1 Externally Synchronized 3.1V/600mA Step-Down Regulator Figure 4 shows an application for low switching-frequency noise. The LTC3404 is synchronized to an external clock signal whereby Burst Mode operation is disabled automatically. This provides constant-frequency operation at lower load currents, reducing the ripple voltage. LTC3404 1 2 47pF 3 4 PLL LPF RUN ITH SYNC/MODE VFB VIN GND SW 8 7 6 5 100 1000 DN261 F05 Figure 5. Efficiency vs Load Current for Figure 4’s Circuit (Burst Mode Operation Disabled) VOUT 100mV/DIV AC COUPLED INDUCTOR CURRENT 500mA/DIV VIN = 4.2V VO = 3.1V LOAD STEP = 50mA TO 600mA EXT CLOCK 1.2MHz 4.7µH* COUT* 22µF CER VOUT* 3.1V VIN 2.65V TO 6V CIN* 10µF CER DN261 F04 22pF 10 LOAD (mA) CLP R 0.01µF LP 100k 887k 309k 1.0 *SEE FIGURE 1 Figure 4. Externally Synchronized 3.1V/600mA Step-Down Regulator Data Sheet Download http://www.linear-tech.com/go/dnLTC3404 Linear Technology Corporation 100µs/DIV Figure 6. Load Step Response for Figure 6’s Circuit Conclusion The LTC3404 demonstrates that high switching frequency and low quiescent current can coexist, and thereby opens up a world of new possibilities in the design of batterypowered products.␣ For literature on our Switching Regulators, call 1-800-4-LINEAR. For applications help, call (408) 432-1900, Ext. 2377 dn261f LT/TP 0501 375K • PRINTED IN THE USA 1630 McCarthy Blvd., Milpitas, CA 95035-7417 www.BDTIC.com/Linear (408)432-1900 ● FAX: (408) 434-0507 ● www.linear-tech.com LINEAR TECHNOLOGY CORPORATION 2001